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Special
Feature by Ian Norton: One owner from new, an MG Midget with added Eight
Port !
Well,
nearly 31 years on since acquiring the only thing I wanted (or I could
afford) at that time with four wheels, I’ve finally got the “period”
modified engine that I’d hankered after ever since I saw those
“8-port” bits listed in Leyland ST tuning catalogue back in the mid
70’s. And I only just got the car I wanted too! Six months after placing
my order (accompanied with the due £10 deposit!), the dealer had
forgotten all about me, and with the new rubber bumper model looming in
October, it was unlikely I’d get the car I’d been saving hard for. But
after the old man had had a few words with the dealer in Birmingham, a car
was eventually dragged off a boat destined for Australia! Wrong colour,
wrong wheels, but at least I had my car. And with the addition of a
factory fitted oil cooler too, something not fitted to UK cars.
It
was great, roof down; open top motoring, just the job! But, the old 1275
was really at the end of its life in terms of performance, and was easily
out done by just about everyone else on the open road. But it was just
such a great car, and I couldn’t let it fade away into becoming just a
quaint “old timer”. So, what to do? Well, the last section of the
owner’s handbook references Leyland ST tuning modifications! So off I
wrote to get all the technical stuff. And back came a tuning booklet for
the Midget. It’s just great! Flywheel lightening details, heads, cams,
wheels; you name it. Being an engineer (Physicist actually), I was hooked!
And so began an episode of finance starved experimentation of making the
old timer go a bit quicker. I really wanted one of those 8 ports, but they
were just too expensive at around £300!! And with all the other bits and
pieces it would certainly have broke the bank. So modified 5 porters was
all I could afford. The final, and best engine was from Oselli and which
now resides in my Frogeye and delivers a reliable 86 brakes at the wheels,
which is good fun in a tin can with no brakes!! But this left me short of
an engine for my Midget.
However,
by the early 90’s it was due a little TLC and so off it went to Brown
and Gammons for some body work. This was followed rapidly by a house move
and my spare time and funds were drawn in different directions, and the MG
sat in a friend’s garage for 6 years! Finally time became more available
and a rearrangement of the garage enabled the MG to return home where I
could begin to refit all the bits and pieces I’d stored in plastic bags.
But what should I do for an engine? Well, onto the net and search around.
I remembered seeing years before some 16 valve overhead cam heads, but the
bonnet would need a big bulge! And anyway, I wanted something period. So
the Arden 8 port was the way to go. It was quite tough finding the link to
Bill Richards but I got there eventually and well, here we are!
I
wanted a car I could drive in the middle of town on a hot summers day.
Something I’d found a problem with when it comes to modified 5 porters!
But a visit to Bill’s place and a friendly chat, defined the project,
which I think Bill was quite excited about it, as his normal work is Mini
based, and the inline variety was novel! Well,
Bill soon got going once the funds arrived! And after 6 weeks or so I
trundled off, trailer in tow, to pick up the finished item. Amazingly not
a single hold up on the M1, M25 or M20! Bill greeted me on arrival and
pointed to the other side of the workshop where my engine sat. It was just
as he had described it (which I cant repeat here!), but suffice it to say
it was awesome. Immaculately painted and built with those two, twin choke
Webers on the special inlet manifold really looking the business. So,
after a chat and a few hints from Bill, I set off home to begin the
installation.
Dropping
the engine in turned out to be the simplest task as the biggest problems
were associated with re-locating the many of the other engine bay
components, not least the heater matrix. This was of course due to the
fact that the carburettors were now on the other side of the engine,
making that side really, really busy. I wanted to make a decent job of
things, so it was some months before everything was sorted and I could get
the car back to Bill for the final stage of fitting an exhaust system and
catch tank. I hired a trailer locally and once again set off South, this
time however getting snarled up in traffic just about all the way there
and on the way back after dropping off the car.
After
a couple of weeks, Bill said it ready and off I set once more to collect
my car. I didn’t want a noisy exhaust, and the exhaust system Bill had
constructed was magnificent and it sounded brilliant! A traffic jam
delayed my trip home and meant I couldn’t return the trailer, which
actually turned out to be a spot of good fortune, as I just couldn’t
start the cat at all (I’d unknowingly managed to flood the engine!). I
used the trailer next morning, on route back to the hire company, to take
the car to my local garage where the problem was diagnosed, to my
embarrassment, and an MOT issued.
I
picked the car up at the next opportunity eager to see how it felt to
drive. Of course, it was running in, so I wasn’t going to drive it hard,
just a gentle run around. The first trip was into town to fill up with
some decent fuel and that was my first pleasant surprise. The car was just
so well mannered around the town in all that stop start traffic, smoothly
rolling along at 1000-1500 rpm with not a hint of snatching, just so
different from my 5-port. Then off I ventured onto the A roads to put a
few miles on the clock before checking for fluid leaks etc. Bill had set
the distributor timing for 31 degrees of advance through the rev range,
which later proved to be a little too much for the engine. However it just
meant the car felt a little cammy up to 3000 where it just took off even
with the slightest of throttle and where one felt it would just keep
going! But the initial impression was that the engine was really strong,
smooth and taught, and I couldn’t wait to get some miles under its belt
to enable the final tune up at Peter Baldwin’s rolling road.
After
about 500 miles and an oil change I made the appointment and set off to
Cambridge for the tune up. That was quite an experience in itself; driving
on the rolling road and observing Peter do his stuff. He soon diagnosed
the timing issue, but Bill’s jetting was spot on! The distributor was
adjusted to give 26 degrees of advance at 5800 rpm where the car delivered
140 bhp. That’s about 30 up on my 5-port! Well, the trip home was quite
exciting. Although the engine was quite flat at low rpm, being now 6
degrees retarded at idle, once it got over the 3000 rpm mark it really
wanted to go and keep going.
Since
then, Bill has reworked the timing so that there are 6 degrees of advance
at idle with a further 20 degrees through the rev range. This has done
wonders for the power distribution and the cam effect is drastically
reduced. The car is just great to drive, however you want to drive it;
easily lives with modern day traffic, and can show a clean pair of heels
to most of its contemporaries! In my opinion, the Arden head should have
been a natural factory upgrade to the engine, at least in inline format
anyway.
Great
job Bill!
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